2018:Drivetrain

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1/7/2018

After the strategy discussion, we were told to keep defense in mind along with offense, after experimenting, strategy was reassured that the drivetrain would make it up the ramp and the robot wheels would stay stable

After lunch we conducted tests with the 2017 and 2014 drive bases with the ramp and the conduit hump and determined that the 2017 drive base as is would not work however the 2014 drive base would due to ground clearances.

Concept study on wheel hight on the platform

modifications to the 2017 drive base to resolve previous issues

1/6/2018

Made several drawings of different sized wheels and height of the bumpers; comparing it to the ramp.


4 inch wheels and 2 inch height

4 inch wheels 2 inch height

6 inch wheels 1.5 inch height

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6 inch wheels 2 inch height

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8 inch wheels 2 inch height

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4 inch wheels 1.5 inch height

4 inch wheels and 1.5 inch height

We could modify last year's drive base by changing the length, and the frame height from the ground. We can adapt it to any size based on what the other teams decide they want. This was the idea has been tested already last year and we know it is fast.

http://penfieldrobotics.com/wiki/images/6/69/A001_Final_Robot_Assembly_-_Larry.png

These are our notes comparing different size wheels and sizes of things on the field to possible drive train sizes.


Notes